forked from forks/qmk_firmware
next_usb: Fix next_kbd_set_leds()
This commit is contained in:
parent
6147f5705a
commit
9b99f8f864
|
@ -59,10 +59,16 @@ static inline void query(void);
|
|||
static inline void reset(void);
|
||||
static inline uint32_t response(void);
|
||||
|
||||
#define out_hi_delay(intervals) do { out_hi(); _delay_us(NEXT_KBD_TIMING * intervals); } while (0);
|
||||
#define out_lo_delay(intervals) do { out_lo(); _delay_us(NEXT_KBD_TIMING * intervals); } while (0);
|
||||
#define query_delay(intervals) do { query(); _delay_us(NEXT_KBD_TIMING * intervals); } while (0);
|
||||
#define reset_delay(intervals) do { reset(); _delay_us(NEXT_KBD_TIMING * intervals); } while (0);
|
||||
/* The keyboard sends signal with 50us pulse width on OUT line
|
||||
* while it seems to miss the 50us pulse on In line.
|
||||
* next_kbd_set_leds() often fails to sync LED status with 50us
|
||||
* but it works well with 51us(+1us) on TMK converter(ATMeaga32u2) at least.
|
||||
* TODO: test on Teensy and Pro Micro configuration
|
||||
*/
|
||||
#define out_hi_delay(intervals) do { out_hi(); _delay_us((NEXT_KBD_TIMING+1) * intervals); } while (0);
|
||||
#define out_lo_delay(intervals) do { out_lo(); _delay_us((NEXT_KBD_TIMING+1) * intervals); } while (0);
|
||||
#define query_delay(intervals) do { query(); _delay_us((NEXT_KBD_TIMING+1) * intervals); } while (0);
|
||||
#define reset_delay(intervals) do { reset(); _delay_us((NEXT_KBD_TIMING+1) * intervals); } while (0);
|
||||
|
||||
void next_kbd_init(void)
|
||||
{
|
||||
|
@ -79,6 +85,7 @@ void next_kbd_init(void)
|
|||
|
||||
void next_kbd_set_leds(bool left, bool right)
|
||||
{
|
||||
cli();
|
||||
out_lo_delay(9);
|
||||
|
||||
out_hi_delay(3);
|
||||
|
@ -98,6 +105,7 @@ void next_kbd_set_leds(bool left, bool right)
|
|||
|
||||
out_lo_delay(7);
|
||||
out_hi();
|
||||
sei();
|
||||
}
|
||||
|
||||
#define NEXT_KBD_READ (NEXT_KBD_IN_PIN&(1<<NEXT_KBD_IN_BIT))
|
||||
|
|
Loading…
Reference in a new issue